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<Duality> @zmat yea 9-bits both read and write but I think it'll be to difficult to achieve, we don't have pru's atleast we use a variant without them.
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<Duality> i think you are correct if I want to properly implement the protocol then i'd have to write a driver that plays with the parity while sending out bytes
<Duality> either low level or with direct access from user space? but it needs to be semi real-time
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<set_> I am messing w/ a PWM lib. from @zmatt...
<set_> Does anyone know about connections that should be made for the TB6600?
<set_> I have the datasheet and they are not correct...of course I am using 3.3v instead of sys_5v.
<set_> Maybe pathlib holds no use in Python3 on kernel 5.10.x?
<set_> I had it working and broke something. Blah.
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<set_> Does this funny schematic make any sense: https://wiki.dfrobot.com/TB6600_Stepper_Motor_Driver_SKU__DRI0043 ?
<set_> It is an Arduino but I am using a BBB.
<set_> It is making me ______ and I have trouble being _______.
<set_> It has two PWM connections, a "GPIO" (I guess), and no GND?
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<set_> Okay! New set up!
<set_> Their ideas are not what I can grasp. off to try set_ ideas now!
<set_> maybe the dip switch...
<set_> hmm
<set_> It would help if I knew something! Off to try GPIO60 as P9.12 and not P9.10. Oops.
<set_> Hmm. That is not it either. The code runs and my source does run too but no movement...
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<set_> @zmatt: This is the source I am trying right now: https://pastebin.com/R70P1wAn
<set_> Is it b/c of GPIOD and no use for pathlib w/ gpio?
<set_> Also...where is the Compatibility Layer for handling /dev/bone/?
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<set_> Maybe using a separate chip is a better idea, i.e. like a L298 for stepper functions...
<zmatt> Duality: if you're doing half-duplex rx+tx then you'll have real-time requirements for switching direction, if you're using full-duplex rx+tx you'll need to use separate uarts per direction since you can't (safely) be receiving while changing the parity for transmit
<set_> Working w/ GPIO and PWM is creating an issue...might just be.
<set_> I mean...I do not even know what is in this box so far. Too bad there are not ideas circulating. Oh well.
<set_> Back to the ole, drawing board.
<set_> @zmatt: Can I post your older model source on the forums to see if someone can help me w/ the build of this TB6600?
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<set_> The motor is excited. I repeat, the motor is excited.
<set_> Luckily, it was moving slow. It almost broke itself!
<set_> Man. That was exciting! Thank you, @zmatt.
<set_> For some reason, this driver expects no ground or something...
<set_> Just a bunch of wires being fed into themselves via headers... 1. for GND and I guess it is like a switch and not a driver.
<set_> 2. This is the first time I have used a driver w/out GND.
<set_> I feel good.
<set_> opto!
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<set_> GenTooMan: I am making makin' moves again!
<set_> You missed it as I cried for mercy...
* set_ knows that darn /dev/bone/pwm* stuff works!
<set_> Gooey OOey!
<set_> I can only be so smart or it is back to the ole farm w/ me...
<set_> Thank you!
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